Helo, Can someone help me? I couldn't run TMC2208 with F6 where I couldn't find the problem. I tried https://github.com/FYSETC/Marlin1.1.9ForFYSETC_F6_TMC2208 and https://github.com/FYSETC/Marlin-F6 as the application software, but motors aren't working. What is the wrong ? I didn't fixed.
You need to set the jumper for the drive like this:
i tried but did not working Connecting... start Printer is now online. echo:Marlin 1.1.9 echo: Last Updated: 2018-08-01 | Author: (none, default config) echo:Compiled: Jun 3 2019 echo: Free Memory: 3053 PlannerBufferBytes: 1296 echo:V57 stored settings retrieved (643 bytes; crc 47958) echo: G21 ; (mm) echo: M149 C ; Units in Celsius echo:Filament settings: Disabled echo: M200 D1.75 echo: M200 D0 echo:Steps per unit: echo: M92 X101.00 Y100.00 Z400.00 E93.00 echo:Maximum feedrates (units/s): echo: M203 X300.00 Y300.00 Z5.00 E25.00 echo:Maximum Acceleration (units/s2): echo: M201 X3000 Y3000 Z100 E10000 echo:Acceleration (units/s2): P<print_accel> R<retract_accel> T<travel_accel> echo: M204 P3000.00 R3000.00 T3000.00 echo:Advanced: B<min_segment_time_us> S<min_feedrate> T<min_travel_feedrate> X<max_x_jerk> Y<max_y_jerk> Z<max_z_jerk> E<max_e_jerk> echo: M205 B20000 S0.00 T0.00 X10.00 Y10.00 Z0.30 E5.00 echo:Home offset: echo: M206 X0.00 Y0.00 Z0.00 echo:Auto Bed Leveling: echo: M420 S0 echo:Material heatup parameters: echo: M145 S0 H215 B60 F0 echo: M145 S1 H255 B100 F0 echo: M145 S2 H230 B70 F0 echo: M145 S3 H240 B50 F0 echo: M145 S4 H230 B85 F0 echo: M145 S5 H220 B100 F0 echo: M145 S6 H254 B100 F0 echo: M145 S7 H200 B70 F0 echo😛ID settings: echo: M301 P22.20 I1.08 D114.00 echo:Z-Probe Offset (mm): echo: M851 Z0.00 echo:Stepper driver current: echo: M906 X800 Y800 Z800 M906 T0 E800 echo:Filament load/unload lengths: echo: M603 L0.00 U100.00
M122 SENDING:M122 X Y Z E Enabled false false false false Set current 800 800 800 800 RMS current 1436 1436 1436 1436 MAX current 2025 2025 2025 2025 Run current 25/31 25/31 25/31 25/31 Hold current 12/31 12/31 12/31 12/31 CS actual 0/31 0/31 0/31 0/31 PWM scale 0 0 0 0 vsense 0=.325 0=.325 0=.325 0=.325 stealthChop false false false false msteps 256 256 256 256 tstep 0 0 0 0 pwm threshold 0 0 0 0 [mm/s] - - - - OT prewarn false false false false OT prewarn has been triggered false false false false off time 0 0 0 0 blank time 16 16 16 16 hysteresis -end -3 -3 -3 -3 -start 1 1 1 1 Stallguard thrs DRVSTATUS X Y Z E stst olb ola s2gb s2ga otpw ot 157C 150C 143C 120C s2vsa s2vsb Driver registers: X 0x00:00:00:00 Bad response! Y 0x00:00:00:00 Bad response! Z 0x00:00:00:00 Bad response! E 0x00:00:00:00 Bad response! Testing X connection... Error: All LOW Testing Y connection... Error: All LOW Testing Z connection... Error: All LOW Testing E connection... Error: All LOW TMC CONNECTION ERRORok
The TMC2208 on F6 only responds to the Y axis because RX is not interrupted on other axis, but other axis can be set and used, just the M122 will not have the correct return value. So,your driver have Incorrect return or not moving?
eliwong All driver not moving
All driver not moving
Did you choose F6 board in arduino software?
Yes of course but not working