it's working when I moved the stepper to E1 slot and pins to
//#define E0_STEP_PIN 26
//#define E0_DIR_PIN 28
//#define E0_ENABLE_PIN 24
#define E0_STEP_PIN 36
#define E0_DIR_PIN 34
#define E0_ENABLE_PIN 30
//#define E1_STEP_PIN 36
//#define E1_DIR_PIN 34
//#define E1_ENABLE_PIN 30
//#define E2_STEP_PIN 59
//#define E2_DIR_PIN 57
//#define E2_ENABLE_PIN 40
#define E0_SERIAL_RX_PIN 80
#define E0_SERIAL_TX_PIN 81
#define E0_CS_PIN 32
But the motors are making a high pitch sound